Hello, I’m testing a pixhawk 2.4.8 for my first drone project, when I first tested the servo rail a few days ago it worked fine - The servos received power and I could control them through the actuator sliders in Qgroundcontrol. Today however I wanted to do further tests before finishing the installation in my drone, and it doesn’t seem like there’s any power at all - I haven’t changed the set up. I’m powering the servo rail through a Hobbywing Skywalker 40A UBEC/ESC
I’ve tried changing out the ESC to another brand new one however still isn’t working.
I’d be glad of any other troubleshooting tips?
Thanks