Hello everyone,
I’m experiencing some issues with my PX4 flight controller and would appreciate your guidance.
Problem Description: I recently updated to the latest firmware version, and since then, my drone has been experiencing erratic behavior during flight. It tends to drift significantly even when I’m not giving any control inputs, and the stabilizing features don’t seem to be working as expected.
Steps Taken:
- I have calibrated the sensors multiple times.
- I double-checked my PID settings to ensure they are configured correctly.
- I reviewed the logs for any error messages, but I’m not sure how to interpret them.
Request for Help: Has anyone experienced similar issues after a firmware update? Any advice on troubleshooting this problem or insights into potential fixes would be greatly appreciated.
Thank you!