X500V2 Flight Beta tests

As Holybro has announced their X500 kit Version 2 I realized that it is better to open this thread so I put my flight tests. Anyone else who also has the kit with Pixhawk 5x is highly welcome to test and share their flight logs here.

@Vincentpoont2 FYI!

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First round of somehow satisfactory flights are as below. I have made the first one as Flight report.

https://review.px4.io/plot_app?log=50fac13b-cf22-4259-9dca-ceb6f916e17f
https://review.px4.io/plot_app?log=f2b50c49-a5e5-4aea-ae2d-17c74aa0a03a
https://logs.px4.io/plot_app?log=4bd7236b-c02f-4756-8dab-fa1acd4455f0
https://logs.px4.io/plot_app?log=f7b08d90-f681-49e5-a52f-feaecaf0ef27
https://review.px4.io/plot_app?log=6827a6d8-43cb-42b1-8f2a-107d5065d7a5

Did some others today:
It is actually a PR but done with this kit:
This one has the whole compass calibration and I had random Yaw inputs from the controller after the flight. Also GPS2 was not detected and I had to connect and reconnect.
https://review.px4.io/plot_app?log=3e777f48-f01c-4cc8-85b5-4187b2dc8ee8
https://review.px4.io/plot_app?log=9664382f-7d76-4c10-8da8-e6f72405c014
https://review.px4.io/plot_app?log=9592f531-a5ef-46b2-b61e-b9d91726e54b
https://review.px4.io/plot_app?log=2df741fa-58a4-4456-ad6b-4e13bab381c8
https://review.px4.io/plot_app?log=572b9118-f619-4591-b1a7-116b2f79d0fe
https://review.px4.io/plot_app?log=8abd2d33-9478-42db-86ed-d4212c5e7832

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These were to test NuttX with test code for stm32:Discard data with Parity Errors by davids5 · Pull Request #19446 · PX4/PX4-Autopilot · GitHub :

Was windy so I did not go high that much. But some other interesting things happened like Arming with High throttle and GPS2 which is not connected at the beginning and I have to connect reconnect the plug to recognize it.
https://review.px4.io/plot_app?log=df47acfd-cfc1-4d83-bad7-554cc0689a16
https://review.px4.io/plot_app?log=52525145-8f8a-4e06-a727-eb990e567388
https://review.px4.io/plot_app?log=fe61e1fb-8490-4f75-8bae-765c155b9d23
https://review.px4.io/plot_app?log=aee3f562-a20a-4b3e-9b43-52e822108530
https://review.px4.io/plot_app?log=fdb9f522-1fb5-4bd0-8f9d-1f6692fe4ec9

Tests with 1.15-rc2 and NXP 6XRT:

https://review.px4.io/plot_app?log=3c286dac-c080-414f-b721-feae5135c149

https://review.px4.io/plot_app?log=84c7cb1c-2d7b-4ec2-be0e-e3a7e4c5eba5

https://review.px4.io/plot_app?log=d8405285-dd2e-4d48-9390-021c07a9f780

https://review.px4.io/plot_app?log=9362d09b-543b-47b5-b64e-8ecc2a3c5121

https://review.px4.io/plot_app?log=c77cdbf5-dbdf-48be-b551-168297827b2a

https://review.px4.io/plot_app?log=74583f38-ad63-4f29-b21a-69d0ac374563

https://review.px4.io/plot_app?log=3d31b1f2-0b3c-4cc1-8c76-71a2c32b9e51

https://review.px4.io/plot_app?log=30af89e5-e6fc-406f-b187-2a14fbc14721

https://review.px4.io/plot_app?log=e6ec07ed-acf2-42a9-8481-5b3a483f4c9a

https://review.px4.io/plot_app?log=af7044e0-b21d-4580-98f5-f5be229451c0

Distance sensor seems not being fused:
https://review.px4.io/plot_app?log=4c00e55b-70d7-4005-9483-50d70f02ba65

This one contains EEPROM MTD Error:
https://review.px4.io/plot_app?log=a0394fb0-a09e-49f7-b877-391132e93051

https://review.px4.io/plot_app?log=2d7ac800-2363-4836-ae5c-411496d6d2d2

https://review.px4.io/plot_app?log=4a3e2dd4-2f04-4852-bad3-3512231f2cd6

cc: @Gerald_Peklar