I updated pixhawk firmware 1.9.2 to 1.10.0 and it’s highly unstable and crass my drone not only one time almost everytime when RTL trigger and position accuracy also decresed. How I can go back tto 1.9.2 which most stable version.
Hi can you share some of your flight log of the unstable flight?
I am also interested in this issue.
Long time no see, as Orico stated, may you please share the log??
Sure I’ll send log files asap.